We've been trucking irrigation water from the city treatment plant for a year now and thus have become ecstatic at the prospect of water supplied simply by turning a valve on.
Greiner Pump and Well came out to install our pump and controls. It was a beautiful day for a project.
In a struggle similar to the discovery process of finding a well driller, we had to do some looking to find Greiner. We've been starting local and then growing our search radius as people no-quote and tell us they aren't interested in the project. We're glad these guys were willing to travel all the way from Keota!
Here's our new pump and motor - lots and lots of stainless-steel! The motor is 5hp -3phase and the pump-end has 16 stages.
Here's our pump control room currently. I'm making an insulated enclosure for this area so that it can be heated next winter.
We opted for a VFD (variable frequency) 3-phase motor drive. It was significantly more expensive than a regular on/off control but it allows the pump to generate any flow required without slamming on and off (a problem when the pump is very large).
The VFD has a pressure transducer on the output manifold for monitoring line pressure. The control will then run the pump motor at any rpm required to hold the manifold at the preset pressure. We can crack open a faucet to a tiny trickle and the motor will just barely turn to meet the demand.
This design just makes sense to me in general and has other benefits such as the floor space consumed by pressure tanks. We were able to use a small 30-gallon pressure tank, which only has the job of providing some water flow for the 1/2-second or so that the pump takes to start.
The pump guys had calculated the necessary pressure tank size for a conventional on/off control of this flow rate and it would have been 500-gallons! A lot of the reason for this difference is that most motor damage/wear is from excessive start cycles.
If I had a conventional on/off system and was just opening a faucet to a trickle, this huge pump would slam on, instantly provide a large volume of flow that has to go somewhere (into the pressure tank) then, it would shut right back off, repeating the cycle over and over. A huge tank would be needed so that the pump could at least stay on for a minute or two. The VFD eliminates all of that.
Kudos to the Greiner crew for surviving the pipe installation process! My concrete floor appeared to be roughly 12" thick with a 24" wide footing along both sides - that's a 6" PVC conduit that they had to run through it! I guess concrete was either really cheap or really easy to make in 1948 when this building was put up.
Here's the capped and finished well casing out back, I thought it turned out pretty good. We've had a few rains since which have helped to settle out the dirt so I can figure out where the grade needs to be.
Eager to get our greenhouse storage-tank filled, I rolled out our brand new fire-hoses. We opened the valve up and noticed one of the hoses had a 1" rip in the side. The well has so much flow that it was still filling the greenhouse tank at a VERY fast rate despite the leak blowing out in the yard. A problem for a different day.